NTSB Identification: FTW71FQG45
14 CFR Part 91 General Aviation
Aircraft: BOEING A75N1, registration: N75262
----------------------------------------------------------------------------------------------------------------------------
 FILE    DATE          LOCATION          AIRCRAFT DATA       INJURIES       FLIGHT                        PILOT DATA
                                                               F  S M/N     PURPOSE
----------------------------------------------------------------------------------------------------------------------------
3-4531  70/11/24   TAHOKA,TEX          BOEING A75N1        CR-  0  0  1  MISCELLANEOUS             AIRLINE TRANSPORT, AGE
        TIME - 0705                    N75262              PX-  0  0  0  FERRY                     44, 13000 TOTAL HOURS,
                                       DAMAGE-DESTROYED    OT-  0  0  0                            3500 IN TYPE, INSTRUMENT
                                                                                                   RATED.
        NAME OF AIRPORT - TAHOKA
        DEPARTURE POINT             INTENDED DESTINATION
          TAHOKA,TEX                  EDCOUCK,TEX
        TYPE OF ACCIDENT                                         PHASE OF OPERATION
           PROPELLER/ROTOR FAILURE: PROPELLER                       TAKEOFF: INITIAL CLIMB
           COLLIDED WITH: DITCHES                                   LANDING: ROLL
        PROBABLE CAUSE(S)
           POWERPLANT - PROPELLER AND ACCESSORIES: BLADES
           MISCELLANEOUS ACTS,CONDITIONS - MATERIAL FAILURE
           PERSONNEL - MAINTENANCE,SERVICING,INSPECTION: INADEQUATE MAINTENANCE AND INSPECTION
           MISCELLANEOUS ACTS,CONDITIONS - VIBRATION,EXCESSIVE
        FACTOR(S)
           PILOT IN COMMAND - INADEQUATE PREFLIGHT PREPARATION AND/OR PLANNING
           MISCELLANEOUS ACTS,CONDITIONS - PREVIOUS DAMAGE
           MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD FAILURE
        EMERGENCY CIRCUMSTANCES - FORCED LANDING ON AIRPORT/SEAPLANE BASE/HELIPT.
                                  PROP/ENGINE VIBRATION
         FIRE AFTER IMPACT
        REMARKS- 8 INCHES OF 1 PROP BLADE FAILED,SEPARATED. UNABLE TO CTL LDG. ROCK NICKS IN BLADE.
Full narrative is not available


​​​​​​