NTSB Identification: CEN15LA233
On May 15, 2015, about 0840 central daylight time, a Cessna T206H airplane, N164CS, overran the end of the runway, following a rejected takeoff from the Piggott Municipal Airport (7M7), Piggott, Arkansas. The airline transport rated pilot received minor injuries and the airplane was substantially damaged. The airplane was registered to and operated by Mid Continent Aircraft Corporation, Hayti, Missouri, under the provisions of the 14 Code of Federal Regulations Part 91 as a cross-country flight. Visual meteorological conditions prevailed at the time. The flight was originating at the time of the accident and was en route to the Walnut Ridge Regional Airport (KARG), Walnut Ridge, Arkansas.
The pilot reported that he planned on departing 7M7's runway 18, and the airplane was configured for a no-flap takeoff. About 1,000 feet down the runway, he rotated for takeoff. When the airplane was about 20-30 feet in the air, the engine "surged", and then lost power. The airplane settled back on to the runway; however, it was traveling too fast to stop on the remaining runway. The airplane came to rest in an irrigation ditch near the runway. The airplane was equipped with air bags, and the pilot's airbag deployed during the accident.
The initial examination of the airplane revealed substantial damage to the left wing and fuselage. The airplane was recovered from the ditch; however, the airplane received extensive damage during the recovery, including separation of the empennage from the fuselage.
The airplane was a 2014 Cessna turbo Stationair (T206H), powered by a Lycoming TIO-540-AJ1A, six-cylinder reciprocating engine, rated at 310 hp. The airplane's "hobbs" meter read 113.6 total flight hours. The airplane was equipped with a Garmin G1000 avionics suite; the engine monitoring data was downloaded from the unit. A review of maintenance records revealed the most recent manufacturer's inspection was completed on March 30, 2015 at a hobbs time of 96.1 flight hours.
The NTSB Investigator in Charge (IIC), a Federal Aviation Administration (FAA) Inspector, and technical representatives from the airframe and engine manufacturers, examined the airplane at a salvage yard facility located in Clinton, Arkansas.
A visual examination of the engine did not reveal any anomalies, so an engine run was planned; however, damage to the airplane's engine mount and propeller limited the test run to low power settings. During the test run, a malfunctioning left magneto was discovered. A review of the engine's maintenance records revealed the left magneto had been replaced at a hobb's time of 98.0 hours.
The engine was separated from the airframe and shipped to Lycoming's engine facility located in Williamsport, Pennsylvania. The engine's left magneto was replaced with a factory test unit and the engine was prepped, and placed in an engine test cell. The NTSB IIC and technical representatives then conducted an engine test run. No abnormalities were noted during the engine test run.
The engine's fuel injection servo unit was removed and sent to Precision Airmotive, LLC, for examination. The examination was conducted under the supervision of the NTSB, with technical representatives from the airframe and fuel servo manufacturers. The fuel servo was bench tested; the unit tested satisfactory, with no performance abnormalities noted. Disassembly of the unit revealed two separation areas on the fuel diaphragm, which failed to show up during the bench test.
The original left magneto and the replacement magneto, which was on the engine at the time of the accident, were shipped to Champion Aerospace facility in Liberty, South Carolina. The NTSB IIC and technical representatives from Textron Aviation (Cessna) and Slick Ignition systems examined the magnetos. The original magneto was placed on a bench test machine; the magneto appeared operational with no abnormalities noted. The magneto on the engine at the time of the accident was then bench tested. The magneto initially displayed normal ignition spark; however, as the rpm increased, the spark became erratic and failed at times to produce spark on all (six) terminals.
The failed magneto was then disassembled; small bits of plastic like material was found inside the magneto consistent with the magneto's rotor. The rotor arm attached to the plastic rotor was out of position and could turn independent of the rotor. The contact points inside the magneto cap showed abnormal wear. Parts from inside the magneto were laid out on a table. A section of a drill bit, about 3/8 inch long, was among the pieces found inside the magneto.
During maintenance and prior to installation of the magneto to the engine, a timing pin (Slick T-118 Magneto Locking pin) is used to time the magneto. The section of drill bit approximated the diameter of the timing pin.
The accident data from the engine monitor was reviewed. Three areas of EGT (exhaust gas temperature) spikes were noted. Two spikes before the takeoff roll were attributed to the pilot conducting the 'before takeoff' magneto checks. The third spike happened during the takeoff and just before a reduction in engine rpms. The data is consistent with the left magneto failing during the takeoff.