THE EXPERIMENTAL HOMEBUILT AIRPLANE HAD JUST REACHED CRUISE ALTITUDE WHEN THE ENGINE FAILED. THE PILOT EXECUTED A FORCED LANDING TO A CORNFIELD AND THE AIRPLANE WAS SUBSTANTIALLY DAMAGED. EXAMINATION OF THE ENGINE REVEALED THAT THE CRANKSHAFT HAD SEIZED DUE TO THE CRANKSHAFT HAVING NO END PLAY, AS REQUIRED. THE CRANKSHAFT MAIN BEARING HAD ALSO FAILED ALLOWING THE DOWEL RODS TO SCORE INTO THE CRANKSHAFT. THE LOGBOOKS WERE INCOMPLETE; THE PERSON WHO INSTALLED THE CRANKSHAFT COULD NOT BE DETERMINED.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
Index for Aug1994 | Index of months