On January 19, 2011, at 1134 central daylight time, a Sikorsky 92A helicopter, N920AL, experienced a flight control malfunction and sustained minor damage during initial descent for landing to Air Logistics Galliano Heliport (2LS0), Galliano, Louisiana. Visual meteorological conditions prevailed and a company flight plan was filed for the 14 Code of Federal Regulations Part 135 non-scheduled passenger flight. The three crewmembers and 15 passengers were not injured. The flight originated from an off-shore helipad at Green Canyon 858 in the Gulf of Mexico, with 2LS0 as its intended destination. Use your browsers 'back' function to return to synopsisReturn to Query Page
During the initial approach into 2LS0, as airspeed reduced through 70 knots, the helicopter began an uncommanded right yaw of more than 100 degrees that could not be stopped by application of left anti-torque pedal. The crew immediately lowered the nose to regain airspeed and streamline the aircraft. They diverted to South Lafourche Airport (GAO), Galliano, Louisiana, and performed a successful roll on landing, touching down at 72 knots, utilizing differential braking to maintain runway heading.
An after landing inspection showed that the tail rotor pitch change beam retaining nut, pitch beam retaining washer, and associated screws and washers were missing. The tail rotor hub and paddles remained attached to the pitch change links and the pitch beam assembly and did not depart the helicopter.
Recent maintenance had been performed to remove and replace the pitch change shaft. Following that maintenance the tail rotor pitch change beam retaining nut and pitch beam retaining washer had been reinstalled and the retaining nut had been torqued to the required value. All of the operator’s mechanics said they thought that all the maintenance items had been performed correctly and they did not notice anything odd or out of place.
Following this incident the manufacturer conducted tests on an exemplar assembly that showed it was possible for the pitch beam retaining washer to be misaligned on the spline and have it partially engage the shaft teeth as the retention nut was rotated and tightened. With the locking washer misaligned, it turned approximately 90 degrees clockwise as the retention nut was being preloaded. At that point the locking washer partially engaged the spline teeth and remained in the cocked condition until the full amount of torque was achieved. The gaps created by the cocked condition and the thread protrusion of the pitch beam retaining nut were visible and measureable. The post-test condition of the teeth on the locking washer included barely visible evidence of the misalignment against the shaft splines.
The manufacturer subsequently issued a change to the aircraft maintenance manual which included additional confirmation of proper alignment of the pitch beam retaining washer and a check for thread protrusion of the pitch change shaft above the tail rotor pitch beam retaining nut.