On August 8, 2007, about 1727 Alaska daylight time, a float-equipped Cessna 185 airplane, N720, sustained substantial damage when it nosed over during a forced landing following a loss of engine power, about 2 miles north of Bethel, Alaska. The airplane was being operated as a visual flight rules (VFR) Title 14 CFR Part 91 positioning flight by the U.S. Department of Interior, Aviation Management Directorate, Anchorage, Alaska, when the accident occurred. The solo commercial pilot was not injured. Visual meteorological conditions prevailed, and company flight following procedures were in effect. Use your browsers 'back' function to return to synopsisReturn to Query Page
During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), on August 9, the pilot related that the accident flight was the first flight after a 100-hour inspection. He said that the purpose of the flight was to reposition the airplane to its mooring site, about 2 miles from the maintenance facility. He added that the repositioning flight would also serve as a postmaintenance operational check flight following the 100-hour inspection.
The pilot reported that after an uneventful takeoff, he climbed the airplane to about 500 feet agl, and began to configure the airplane for cruise flight. He said that soon after leveling at 400 feet agl, he noted a rough running engine, followed by a gradual reduction in engine rpm. He said that engine emergency procedures did not remedy the engine roughness, which was followed by a rapid loss of engine power, and subsequent loss of altitude. The pilot reported that he was unable to maintain level flight, and he selected a small pond as a forced landing site. After touchdown on the pond, the airplane's floats collided with the soft, tundra-covered shoreline, and the airplane nosed over, sustaining substantial damage to the left wing, right wing lift strut, empennage, and fuselage.
Two air safety investigators from the Aviation Management Directorate, in Boise, Idaho, traveled to the accident scene on August 11, 2007, and examined the airplane. The investigators reported that an inspection of the airplane revealed that the fuel selector handle had been inadvertently reinstalled incorrectly during the recent 100-hour inspection. The investigators said that when the fuel tank selector was placed in the "Both" position, it actually turned the fuel supply off.
The main fuel valve selector handle is located on the floor, between the two front seats. The three-position handle allows the pilot to select fuel to the engine from either the right or left fuel tanks, or both. The airplane's fuel selector valve assembly is located about 6-inches beneath the airplane's floor. A 6-inch long rigid cable assembly connects the fuel selector valve to the fuel selector handle. Both ends of the rigid cable assembly use a keyed cog, which is designed to prevent maintenance personnel from installing the fuel selector handle incorrectly. The fuel selector handle assembly, along with the rigid cable assembly, were removed from the accident airplane and shipped to the NTSB IIC in Anchorage for inspection.
On September 20, 2007, in Wichita, Kansas, the NTSB IIC, along with a senior Cessna Aircraft Company engineering specialist, examined the fuel selector handle and cable assembly that was removed from the accident airplane. The inspection revealed wear marks, with minor rounding of the keyed (male) end of the cog on the rigid cable assembly. In addition, wear marks and a slight elongation of the (female) receptacle on the fuel valve handle was also noted. The combined wear on both the keyed cog on the rigid cable assembly, and wear of the keyed cog on the fuel selector valve handle, inadvertently allowed the installation of the fuel selector handle 180 degrees from the correct position. The Cessna engineer provided the NTSB IIC with a new fuel selector valve handle for comparison. When the new fuel selector handle was fitted on rigid cable assembly, it could only be installed in the correct position, and not 180 degrees from the correct installation.