NTSB Identification: DEN08LA066.
The docket is stored in the Docket Management System (DMS). Please contact Records Management Division
Accident occurred Tuesday, March 18, 2008 in Las Vegas, NM
Probable Cause Approval Date: 08/28/2008
Aircraft: Robinson R22 BETA, registration: N3055N
Injuries: 2 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

Both the terminal forecast (TAF) and the Automated Weather Observation Station (AWOS) reported the wind to be from 020 degrees, but the TAF reported wind velocity to be 10 knots, whereas AWOS reported it to be 15 knots with gusts to 20 knots. As the helicopter approached the airport, the student told the instructor he would like to practice a 180 degree autorotation. The maneuver was begun from 1,000 feet agl (above ground level), but due to poor rpm and speed control, the instructor assumed control of the helicopter and advised the student he would demonstrate the proper technique. The instructor said he kept the rpm "in the green" and kept the airspeed above 65 knots, but realized the helicopter was descending "at an unusually high rate of descent." As he rolled out to level, "it felt as if we had a huge downdraft that was pushing us towards the ground." The instructor added throttle and began to "pull all the power available." Lift was not sufficient to overcome the descent rate. Just prior to impact, the pilot applied slight aft cyclic control. The helicopter struck the ground, bounced, and continued to fly with some forward momentum. The instructor then landed the helicopter. Post-impact inspection revealed the skids were spread, the engine mounts were bent, and part of the pilot's window had popped out. The instructor said that at no time did the LOW ROTOR RPM horn sound.

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

An inadvertent settling with power, and the instructor's failure to maintain control of the helicopter, resulting in a hard landing. Contributing to the accident was the downdraft.

Full narrative available

Index for Mar2008 | Index of months