NTSB Identification: DEN05LA123.
The docket is stored in the Docket Management System (DMS). Please contact Records Management Division
Accident occurred Sunday, August 07, 2005 in Albuquerque, NM
Probable Cause Approval Date: 01/31/2006
Aircraft: Forbes Rutan Long EZE, registration: N16WF
Injuries: 1 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On final approach to the runway, the pilot lowered the landing gear and visually inspected it through the sight glass to make sure it was down and locked. About 20 seconds later, there was a sudden and total electrical failure and the engine lost power. The pilot switched from the MAIN battery to the AUX battery in an attempt to restore electrical and engine power, but left it selected for only about 2 to 3 seconds. He then switched back to the MAIN battery and concentrated on the emergency forced landing. He could not recall if the propeller was windmilling at the time (a windmilling propeller would be necessary to start the engine using AUX battery power). The pilot made a forced landing on an access road and collided with a wall causing substantial damage. The airplane was equipped with a dual electronic ignition system, not magnetos. A constant source of electrical power was required for ignition. In the event of an electrical power loss, the engine would lose power. An FAA avionics inspector said the 5-amp main fuse had opened, probably due to a shorted wire inside the master relay, resulting in an over-current condition. This caused the master relay to de-energize and cut power to the bus. The alternator, which was tested to 10.5 volt output, has a nominal output of 13.8 volts. Minimal output to charge the battery is 12.5 volts. The FAA inspector's statement noted that the cockpit-mounted master switch activated the positive side of the master relay solenoid. Standard industry practice was to wire the positive side of the master relay to the unfused input from the battery, and then switch the negative side using the master switch. Some commercially available solenoids have the positive terminal wired to the battery input.

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

a total electrical failure due to a short in the master relay, causing the main fuse to open. Contributing factors included an inadequate electrical design by the airplane's builder, a low-output alternator, a cement wall, and unsuitable terrain on which to make a forced landing.

Full narrative available

Index for Aug2005 | Index of months