NTSB Identification: LAX00TA212.
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Accident occurred Thursday, June 01, 2000 in AUSTIN, NV
Probable Cause Approval Date: 07/15/2002
Aircraft: Piper PA-18-150, registration: N4872A
Injuries: 2 Minor.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this public aircraft accident report.

The pilot reported that he had been monitoring an increase in the fuel burn rate over a period of time. His normal leaning procedure for best power operating from 5,800 feet mean sea level required more mixture control travel. On the day of the accident, it was the second time that the engine had failed to respond to throttle input. The subsequent loss of engine power occurred low to the terrain. Post accident examination of the carburetor revealed a black composite float that felt heavier than normal. One pontoon exhibited light damage to the smooth shell. The engine spark plugs were lightly fuel sooted. According to Precision Airmotive Corporation "mandatory" Service Bulletin MSA-1(replacement of composite floats with metal floats), the type certificate holder of the carburetor, states that; "field reports indicate that composite floats may be absorbing fluid and sinking," replace the existing composite float with a metal float. A sinking float may result in disruption of fuel flow to the engine, Precision Airmotive therefore considers the replacement of composite floats with metal floats mandatory. Compliance is optional for 14 CFR Part 91 operators.



The National Transportation Safety Board determines the probable cause(s) of this accident to be:

Loss of engine power caused by a fuel soaked float pontoon causing an over rich fuel/air mixture, in a critical phase of flight.

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