NTSB Identification: MIA93LA131.
The docket is stored in the Docket Management System (DMS). Please contact Records Management Division
Accident occurred Thursday, May 27, 1993 in MYAKKA, FL
Probable Cause Approval Date: 09/26/1994
Aircraft: CESSNA 210K, registration: N8278M
Injuries: 2 Uninjured.
NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.
During cruise flight the engine failed and the pilot executed a forced landing to a field. During the landing the nose gear and main gear collapsed. The No. 2 cylinder connecting rod was found failed. Examination of the failed connecting rod did not determine the cause of failure due to excessive damage.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The failure of the No. 2 piston connecting rod for undetermined reasons. Contributing to the accident was a forced landing to unsuitable terrain. Full narrative available
Index for May1993 | Index of months