NTSB Identification: LAX97LA098.
The docket is stored in the Docket Management System (DMS). Please contact Records Management Division
Accident occurred Friday, January 31, 1997 in SCOTTSDALE, AZ
Probable Cause Approval Date: 02/02/1998
Aircraft: Bellanca 17-30A, registration: N6638V
Injuries: 2 Minor.
NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.
The pilot contacted the FAA control tower while on approach to his destination and was advised to report on a long right base for runway 21. The pilot reported about 4 miles from the airport the engine suddenly dropped to idle, it did not quit, and the throttle had no effect on the rpm. He stated that he immediately looked at the fuel gauge and noticed approximately 1/4 tank. He tried switching tanks, but could not get a restart or increase from idle. According to FAA inspectors, the fuel selector was found on the left outboard fuel tank and the outboard fuel tanks were found empty.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: fuel exhaustion due to the pilot's improper fuel management. Full narrative available
Index for Jan1997 | Index of months